Our Yami high thust kicker appears to be over heating. The pisser appears to be working, if not super strong but nothing that would cause great concern. At lower rpm it appears to be cooling adequately but during periods when the infamous JDF current is racing and the kicker has to be run at higher rpm to push through it, it appears to develops symptoms of running hot.
It gets a little white smoke (we don't think it is steam) and you can smell it a little and the head/block feels very hot. I assume it is burning off oil and corrosion resistant spay on the outside of the motor. The motor oil itself is right up and clean. The motor does not get flushed with fresh water all that often compared to motors that are trailered and flushed daily as it stays in the ocean for the season. There is a lot of weed out there recently and we wondered about something being sucked into the cooling system and partially blocking it???
The motor was bought new in Aug of 2014 and does not have a lot of hours on it, but is still on its original water pump. Our plan is to get a new T-stat and water pump/impeller rebuild kit and pull the leg and replace them. Then run the salt away injector system through the motor with fresh water.
I am hoping that fixes it as I really would not like to have to pull the head etc. and clean out all the little tiny cooling passages and miss the end of our very short fishing season this year. May not want to even take that job on ourselves and may have to get a pro to do it, if it is necessary.
Any suggestions or thoughts?
It gets a little white smoke (we don't think it is steam) and you can smell it a little and the head/block feels very hot. I assume it is burning off oil and corrosion resistant spay on the outside of the motor. The motor oil itself is right up and clean. The motor does not get flushed with fresh water all that often compared to motors that are trailered and flushed daily as it stays in the ocean for the season. There is a lot of weed out there recently and we wondered about something being sucked into the cooling system and partially blocking it???
The motor was bought new in Aug of 2014 and does not have a lot of hours on it, but is still on its original water pump. Our plan is to get a new T-stat and water pump/impeller rebuild kit and pull the leg and replace them. Then run the salt away injector system through the motor with fresh water.
I am hoping that fixes it as I really would not like to have to pull the head etc. and clean out all the little tiny cooling passages and miss the end of our very short fishing season this year. May not want to even take that job on ourselves and may have to get a pro to do it, if it is necessary.
Any suggestions or thoughts?
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